Buckling Analysis with Guyed Tower of 500kv Transmission Line
With guyed Tower(type:LM21) of 500kV transmission lines, the joint bar of tower body and stayguy had been deformed severely in the process of operation. We did the buckling analysis in different load condition with application of finite element method. The results revealed that the nether cross arm yielded under load of cladding ice and imbalance tension. Then we do experiment with prototype tower and acquire corresponding datum. By contrasting the theory results and experimental datum, we can make sure that this method of analsing tower is exact and proper. Finally, we setted out improvemental means that to change material specification of the nether cross arm from 80mmx80mmx6mm to 120mmxl00mmxl4mm. By this insteading, the intensity and deformation of tower have met designing requirements.
SOOkV transmission line guyed tower buckling analysis prototype experiment
Wei Kong Jian Dang
College of Civil Engineering Northeast Dianli University Jilin, China
国际会议
太原
英文
376-378
2010-10-22(万方平台首次上网日期,不代表论文的发表时间)